About VK5ZM

Another Ham who was bitten by the Fox Hunting Bug in the early 90's. Participated in numerous National DF championships and likes nothing more than the challenge of finding *any* hidden radio transmitter. Loves to build all of his own equipment, QSO's on homebrew gear is much more exciting than black-box operation. Has been involved in HAB experiments since 2010. Goal is to fill his Toyota Hilux so full of DF gear that he has to buy a Landcruiser.... Approximately half way there.

New Switches

With the lights upgraded it was about time I found a decent switch to sit on the dash board and activate the spotties.

I’d noticed recently that Narva offered a series of “Carling” styled switches that came with blue indicators that looked about the right size.  I hate blue lights in cars, it hurts the eyes and causes fatigue.

There are three switch positions in the car that measured up close to a standard 32mm x 26mm DIN cutout.

A bit of google foo and I find online suppliers that can offer the same switch with various printing with a range of indicator colours.  I ordered Green to match the rest of the console.

They fit perfectly.

There was only just a tiny amount of filing required to squeeze the switch into the cutout, perhaps a millimetre or two.   Anyway the effect is great.

The switch has two indicators, the lower that comes on when the lights are activated and a second under the symbol when you activate the switch.   This required a bit of thinking as to how to wire it properly and an additional diode to get it to work with the relay kit.   I should at some stage draw up the circuit diagram.

My only complaint is the LED’s are far brighter than the equivalent incandescent bulb which means even when dimmed by the rheostat they are still too bright.  I’ll be pulling the switch out and wiring a separate resistor in series to lower the brightness further.  Hmm… that might require a transistor and zener, time to get that piece of paper out.

Oh and while I was ordering one “spot lights” switch I grabbed a few others that I thought I might want so there is now a small collection ready and waiting for further improvements.

Let there be Light !

Since rebuilding the engine and putting a Turbo on it one thing was abundantly clear, I could now go much faster than I could see.

After some 20 years the original 7″ x 5″ sealed beams (yes sealed beams!) were not cutting the mustard anymore.  They were dim to say the very least and only 20 years behind headlight development.  After driving a more modern car with good headlights when I jumped back into the Hilux the difference was clear to see.

Now modifications to car headlights have to be done carefully with the right parts or you can see your car defected and taken off the road here in South Australia.  Not to mention the driver also gets fined.   Getting these defect stickers taken off your car means a “roadworthy” and is a costly exercise.  So make sure you know your local regulatory requirements before embarking on your own head light upgrade.

After a bit of google foo I found some replacement headlight kits that were ADR-46/00   approved.   This approval essentially means that the headlights when installed and aligned correctly will not cause glare to oncoming drivers.   The headlights I chose were from Narva and were part of their “Freeform Headlamp Series” (click) specifically the Narva 72024 Headlight Kit.

These Narva headlights accept a standard H4 insert, so that meant I was also free to choose a lamp of my liking.

After even more google foo I settled on the Narva Plus 120 lamps since they claim 120% more light than standard bulbs for the same power (55/60W), but more importantly they are ADR 51/00 approved.  This means not only are the headlamp assemblies approved but so are the lamps.  No chance now of a defect notice !

Fitting these lamps was not difficult.  All that was required was to release the front grill to allow the stainless steel surrounds that hold the globes to be undone, slip the old ones out and slip the new ones in.  The rubber dust seal requires a little attention to detail, but is not difficult to seat.   I didn’t need the integral parking bulbs so these were swapped for the rubber plugs.  Then just plug in and put it all back together.

  

Now I have also been very fortunate to have been given a set of spot lights when one of our club members was cleaning out his Shed recently.  So it was also time to install these on the bull bar to round out the upgrade.

So a pair of Lightforce Striker 170’s were installed on the bull bar.  At 100W a piece these should throw some serious light down the road.  The wiring harness that came with the kit was actually not too bad, a couple of minor modifications and it was dropped into the engine bay.   Wiring up a carling swtich on the other hand will be a subject of a subsequent post.  I’m glad I’m an engineer and know a thing or two about electricity, lets just say a diode was required to make the lamps in the switch work correctly.  Watch this space.

So the end result ?  You can see for yourself below.

Now it is very important that your lights are aligned properly.  I simply used a blank wall, mark the centre of the beams and drive backwards 7.5m and then align them as per the operators handbook.   Thankfully I found some flat ground in a local supermarket car park, I’m certain the security guards were a little confused for a bit what I was doing.  Anyway the headlights were aligned enough for me to drive it to somewhere that can do it properly.

The proof however they say is in the pudding.

Having driven it tonight some 200 kms along the South Eastern Freeway to Tailem Bend and back, I can only say that I’m seriously impressed with the new headlights.   The beam and patterns are quite simply great, the additional lumens from the lamps (some 120% greater than standard) throws the low beams out there an additional 40m.   On high beam the light shifts forward well past 150m and throws additional light to the sides.  The light back from road signs is not offensive and cat’s eyes on the road illuminate well.  Yes this is a great “legal” upgrade just on it’s own.

I’ve not gone for any of the blue rich white light lamps since I find that fatiguing when driving long distances at night.  I’d guess the colour temp of the current lamps is around 3000-3200K, it’s well above your typical 2500-2700K “yellow” sealed beams and below the w**ker with the “white” lights at 3700K and beyond.

I also got the chance to arc up the driving lights when no other cars were around, those will definitely burn the ears off any bunnies or roos that are sitting by the side of the road.  On long straights I’m seeing reflectors and signs lighting up some 650-800m down the road.  Man they are bright.  Now to work out how to get a photo.

So at the very begging of this blog post I wrote;

“Let there be light” – and there was …!!!

Autotecnica Gauge Disappointment

Well what a disappointment.  After three weeks of wrestling with the Autotecnica Gauges that I bought, I’ve called it a day.  They just don’t work as one would expect and will be ripped out of the car and returned for a refund.  There dummy has been spat !

These gauges certainly looked the part and were of a reasonable price, however their operation, reliability and accuracy were their ultimate failure.

The installation instructions were poor to say the least, just a single piece of paper with rough as guts chicken scratching’s as a guide how to wire them.  This was not a great start. There was no information (or clues) regarding wire gauge, so after measuring less than 100mA per gauge plus sender I decided it was safe to use 28 gauge (0.25mm^2) wire.

Looms were made that connected the oil pressure sender (electronic), boost pressure sender (electronic), coolant sender (resistive) and EGT probe (thermocouple).  Where the wires came close to the engine block they were sleeved in fibreglass everywhere else heat shrink.  In all the job looked nice.

However the Boost pressure gauge measured 3 psi low at full boost (~10psi) which was at least 30% in error.  Results were confirmed using a trusted mechanical pressure gauge. The EGT gauge would every once in a while stop reading anything and sit there and sulk.  The probe was tested by my Agilent multimeter that could read K-type thermocouples.  The water gauge worked perfectly, the oil pressure gauge well that was possessed and did its own thing.  If you watch the next video you’ll see what I mean.

https://youtu.be/xAU8Ox38w5s

So that left me with a working water gauge (nice to have), under reading boost gauge (should have), faulty EGT display (shall have) and weird oil pressure gauge (nice to have).   A total score of 1 out of 4 with all critical systems in the red.

Oh well that will learn me for being cheap.  With luck I’ll get that refund, these gauges certainly did not work as advertised and were not fit for purpose.

I am also very glad that I yanked them when I did.  I borrowed my local car mechanics four post hoist to get at the oil pressure sender when it fell out in my hand. It turns out the brass fitting I’d bought for the oil pressure sender had gone brittle and fractured where it came out of the block.  Nothing an easy out couldn’t rectify, but I’m now very glad this came out in my hand rather than at 100kph on the freeway spraying hot oil over the wheels, engine bay and brakes.  A major disaster averted.

So for now I’ve have settled on a pair of trusty ol’ VDO mechanical gauges, shouldn’t look too bad in the pod.  The pod came with 52 -> 60mm adaptors.  These gauges are a little plain when compared to my previous gauges, but functional is what I’m after at this point.

That at least means I can monitor EGT and Boost properly and make sure that this new engine is looked after.  With these gauges being partially mechanical it will be interesting to bring pipe and heavy wires in from the engine bay.

I also laugh when you have to marry imperial with metric.  The DTS turbo kit dump pipe has a metric O2 sensor port into which I  screw the EGT probe.  My previous Chinese EGT sensors were thin-ish and came with a 1/8 NPT 27 tpi thread, so I was lucky enough to be given a steel pipe reducer that fitted nicely.  Of course VDO don’t like the small probes and have supplied a much larger unit with a 1/4 NPT 14 tpi thread.  So after a lot of searching I found that DTS sell the adaptor (fancy that, on the left) and their HQ was here in Adelaide.

I’m certainly glad I found this little doodad it saved me from having to buy/beg/borrow or steal a 1/4 NPT 14 tpi tap !

Toyota Hilux Engine Rebuild

Well after some 392,000 km’s my Old 1996 Toyota Hilux decided to call it a day in rather spectacular fashion.

On this trip the harmonic balancer spun on the end of the crank shaft, which was a messy situation that would ultimately result in either a proper engine rebuild or permanent retirement of the car.

She came home on the back of a trailer, the first time in 18 years that she’s never made it home on her own.

Now I simply don’t like the newer Hilux models with all their fan dangley new engines that make noise on RF and you can’t drop a spanner between the engine and the body and not see it fall through.  My Hilux had a “simple”  Toyota 3L naturally aspirated 2.8L mechanically injected diesel, this makes it the perfect car for mobile HF and foxhunting, since there is nothing in the car that can make any RF noise (except the alternator brushes).  Besides I’ve owned this car for 18 years now so I know everything that is wrong with it, what’s been replaced and what needed to be fixed.

I had planned on rebuilding the engine at 400,000 kms since it was due a new timing belt and my parents were going away for 3 months so  I could borrow there spare car.  However with a bit of “bush mechanics” and a tube of loctite 660, we (well the royal we) effected a repair on the old engine for the necessary three weeks to tide me over.  When the old girl was backed down the drive way she’d done just over 395,000 kms not a bad innings.

One of my fellow club members Gary VK5FGRY happens to be a retired mechanic with many years of experience and offered to help with a rebuild.  Certainly without his help, knowledge, research, friendship, attention to detail and support I’d have probably not have rebuilt the engine and simply retired the old girl.  I’m glad I didn’t and will be forever grateful of all the hard work and effort that Gary poured into my “rebuild project”.

So the first step was to pull out the engine and see what sort of mess we were dealing with.  Nothing like rebuilding a car in the drive way so here we go.

Yep that is one very dirty, tired, greasy old oil burner.   Mind you she’s *never* had a spanner on the head bolts. I’ve replaced starter motors, alternators, water and vaccum pumps, rebuild front and rear diffs a few times, replaced shockers, springs and bushes, but you get that with any vehicle that is 20 years old.

After researching my options and costs for a local rebuild I decided to send my engine to APA Diesel in Sydney.  The cost of freight and insurance was surprisingly low for a pallet weighing some 170kgs.  So here is what I sent to Sydney, and what I got back 4 weeks later.  The boys at APA Diesel certainly did a nice job, the only piece missing was the sump plug (*grin*) not too bad IMHO.  The frame for the motor on the pallet was custom built for less than $50 in materials.

The difference is quite clearly chalk and cheese.

Ok you might notice that on the exhaust side of the engine a few additional bits have been added.  The original engine made 63kW@157Nm or torque when new, which was barely enough to get the Hilux up the next hill.  It seemed silly to rebuild her and not “tweak” some extra ponies, so some forced induction bits were procured and bolted on.  Part of the reason for me choosing an interstate Engine builder.    The list of what was changed within the engine is long, but in short she’s been built to take the turbo from the ground up.  No point in doing half a job.  I’m expecting something like 80kW @ 250Nm of torque when we finally get her on the dyno in a few months for a tune up, will wait until after the breakin period to find out.

With the engine out that certainly left a gaping hole in the engine bay, especially when we dropped the gearbox and drive shafts out too for some repairs.  There was still a lot of oil around, but nothing a few tins of degreaser and a bit of high pressure cleaning can’t fix.

The gearbox was also leaking a little (ok a lot of) oil from it’s seals and had a faulty gear selector.   At some point in the past the nut on the rear output shaft wasn’t done up tight and had been leaking for a considerable time, the mess 2′ either side of the gearbox on the under body of the car certainly stands testament to the duration of this leak.  Steam cleaner here we come.

Ordering parts online for these old Hilux’s is now days very easy with the car being more than 15 yrs old.  All of the OEM parts manufactures are pumping out cost effective replacements.  It helps that these Hilux’s are popular to rebuild here in Oz.  I ordered new seals, new selectors and bushes for a few hundred bucks and re-sealed the gearbox.  It was not making any noise prior to the build so there was no need to open her up for surgery, just clean up around the outside.  Man did that require some degreaser and high pressure cleaning however.

During disassembly we also found that the input shaft to the gearbox had been nurgled by the previous spigot bearing disintegrating.  Well munted is perhaps a better term, cant use the other vernacular in a public forum, but a picture speaks a 1000 words.  It should be nice and flat without the scallop.

Time to call on another favour from a club member Dennis VK5FDEN who is a fitter and turner by trade, also with years of experience to make a new sleave.  A bit of loctite 660 (this tube got some good use), a good interference fit and some care and we simply increased the diameter of the spigot to the next size up bearing we could purchase.  You should get the idea from these two pictures.

Once the gearbox went back into the car you’d have been hard pressed to realise that the spigot bearing had been changed and the input shaft repaired.  A job well done that is for certain and one that should last the remaining lifetime of the car.

The power steering pump in the old girl snapped it’s bolt a number of years ago while on the Birdsville track.  Not having a convenient fence to steal a bit of wire or enough cable ties, meant the pump spent time on a broken bolt for 300kms which resulted in the pump flogging out it’s mounts. This meant that the pump alignment to the belt was off centre and the belt and pump would make a squeek squeek noise when running.  I was determined that this was not going to continue, so  Dennis also repaired the pump with small bolt that would force the bolt back to where it should be with a lock nut.  At some point the pump may have to come out and be repaired again (or replaced new if I can find one cheap enough), but cross that bridge later.  For now the power steering pump is fixed.

So it was now time to start putting things back together.

As you can see above the engine went back in relatively smoothly.  A bit of giggling and pushing for an hour or so saw the gearbox and engine re-united.  Tyres had to be deflated to get the engine to clear the bull bar since the pipes on the turbo meant additional clearance was required on the hoist.  We managed to clear the bull bar by only 1″ with the tyres fully deflated.

At this point in the build the majority of work was being done by torch light under the veranda late into the night, so taking pictures or videos was a little difficult.  Once the engine went back it in was a straight forward process to hook up the electrics, plumb in all the necessary water lines, fuel lines and oil lines.   Re-fitting of the starter motor was fairly straight forward if not a pain due to clearance etc.

It turns out the airconditioner compressor has a crook bearing so that will have to be fixed at some point in the not too distant future.  We left the belt off to remind us to fix it.

A temporary exhaust was fashioned from the old header pipe, this will need to be “re-worked” at a local exhaust shop.  A while ago I had the exhaust replaced with a 2 1/4″ system which it turns out is perfect for this turbo setup.  Wooo the power.

Drive shafts were put back in, two of the yokes were “notchy” and were overhauled by my local mechanic near work. We’ll leave the discussions about bruised drive shaft mating surfaces for another time.  If we only had the necessary press (*sigh*).

The rebuild process once the engine arrived was a little over 5 days, most of that was spent cleaning, washing and painting parts.  This is a busy time of the year for our radio club, so there wasn’t much time on the weekends prior to do all of the prep work before hand.   In all it’s taken 8-10 days to actual effort to take the engine out, repair and put back in.   Linear time however has been weeks of waiting, the freight backwards and forwards being the longest.  Doing it ourselves has saved a lot in labour costs.

Then all there was time to do was go and drive it, find some big hills and see what difference the turbo makes.  Keeping in mind that this is a brand new engine that still has to be “broken” in, so no thrashing it, no labouring it just let it work and keep pulling.   So maybe sometime next year or the year after it will be “finally broken in” (*grin*).

The_Drive_VK5ZP-9

There are a number of hills in this loop that we just scooted over the top of in top gear at the speed limit, where previously it would have been in 3rd gear having the neck wrung out of it to hold 10 or so kph under the limit.  There is no doubt that the turbo has increased both power and torque considerably.  Before this drive Gary and I did a small loop over the top of Norton Summit up some very steep gradients, but I forgot my antenna so didn’t get it on APRS.

It’s funny too how cars develop gremlins while sitting still.  When driving the car in the big loop above the windscreen wipers decided they wanted to start going along with the washer all of their own accord.  A quick stop at the 24hr car wash (great lighting !) behind the servo saw both the windscreen wipers and washer unplugged.  I’ve a nasty feeling the combination stalk is on it’s way out, otherwise there’s a relay there full of water I’m yet to find.  Nothing that this scribe can’t fix.

Now all that remains is to add my new gauges so I can keep an eye on what the new engine is doing.  All of the senders were added to the engine as we went (EGT, oil and water) just need to find a bit of fuel hose to plumb in the boost.  I found these really nice dual gauges on ebay with electronic senders.  A touch of class while being able to look at all “vital engine statistics”.  The wiring should be complete in a few days.

Now I guess I’d better get back to work and earn a few dollars to pay for my engine rebuild.  Can’t wait for the next fox or balloon hunt to see how much earlier we can arrive on site (*grin*).  Taking it for a any drive puts a smile on your face.

I guess no post is complete without a video;

https://youtu.be/AGnL7_-nhIo

Thanks again to everyone that came to visit and help with the build, I think the comment “It’s amazing that you can learn by holding a light” by Kim VK5FJ is both funny but very true !!!